Fuse that may be ignition circuit blew after changing
alternator belt in Governor’s Harbor on 5/12; Rob bought new fuse but had to
get 50 amps instead of 40 amps, which is what was originally in the motor. Fuse is between starboard-side battery and
the ignition switch, though it is unclear what exactly the name for this fuse
would be. Fuse was originally a large
spade car fuse, recent model; replacement bought at auto parts store. Rob also bought but has not used 40 amp
smaller spade fuses. After replacing
with 50 amp large fuse, motor ran out of Governor’s Harbor, into No Name
Harbor, then for 3 hours to Deep Creek and restarted to go one more hour into Plum
Creek.
Motor ran fine to get out of Eleuthera and roughly half an
hour to anchor at Highborne Cay. Again,
started fine to pull up anchor at Highbourne on May 17, then Rob could tell
fuse had blown because the amp gage read 0 amps and battery levels began to
drop. However, we were still able to
motor another two hours to Norman’s Cay where the motor stopped once lowered to
idle speed and the gages would not work on trying to restart. Other boaters made a fuse for us with 16-gage
wire and spade connectors and suggested inspecting electrical system for any
corrosion. Rob replaced fuse with
makeshift fuse, tightened the alternator belt, tightened a cooling hose clamp
that may have been dripping on another wire connection (involved in this
circuit – goes to distributor cap but unknown need of wire). Visual inspection found no corrosion on any
wiring in engine compartment, but found one spark plug wire was not connected
at distributor cap (meaning we had been running off only three spark plugs for
an unknown known amount of time). Gage
panel was not inspected. Makeshift fuse
worked(!) and motor ran to get off anchor and to lay anchor at Hawksbill Cay.
From Hawksbill to Warderick Wells, had to run motor almost
entire time (roughly four hours) with no problems and we ran the motor
occasionally during the four days at Warderick Wells to recharge batteries for
15 minutes to an hour at a time. Getting
off anchor and for the last half of journey (roughly two hours) to O’Brien’s,
motor ran without issue. Getting off
anchor and for two hours after leaving O’Brien’s Cay, motor ran without
issue. We encountered ~10 foot swells in
the Sound side, so decided to cut through Conch Cut to the Banks side, so boat
was no longer being tossed about. As we
were halfway through a narrow channel, the motor just died as though we had run
out of gas – no sound, no smell, just died though we had ¼ tank of gas. I tried to start motor, where it tried to
turn over but did not start. Second try
and none of the gages worked.
Makeshift fuse had melted the rubber cover and burned
through. Inspection of all terminals on
the amperage gage in instrument cluster are found to be corroded, one at the
level of blueish-green coloring while the other two are lightly corroded. Rob cleaned the terminals after making
another 16-gage wire fuse, which has already been found to make the gages work. As of 5/31, no motor problems detected. We're pretty sure that the gas tank being low and shaken up so much in the high waves just threw out a clump that choked the engine as we have not experienced that problem since and the engine started up without a problem after about an hour and a half of just sitting.
5/30 – The VHF radio has been turned off for the past couple
of days while we have been at anchor, but turned on without trouble. As another boat’s message came across the
radio, I realized that the volume was up way too loud and turned it down. I was able to call the Staniel Cay Yacht
Club, receive their response, switch from channel 16 to 11, and have a brief conversation
with the SCYC. After returning to
Channel 16, I switched the VHF off the way we have been turning it off and on
since buying the boat by flipping the breaker off.
After thinking about the idea that possibly someone might
have heard the boat’s name and would be interested in calling us, I flipped the
breaker switch back on but the radio did not come on. Rob checked that the fuse was still good,
measured the wire coming from the breaker and the wire coming from the radio
with the voltmeter, and found no problems.
After playing with switches, cursing just a bit, and trying new ideas,
Rob found that as long as the VHF is turned off when the breaker is turned on,
the radio has no trouble turning on.
However, when the radio is on and the breaker is turned on, the radio
does not turn on… after six months of doing so.
5/31 – The Garmin GPS/depth sounder started intermittently beeping
with “low voltage” alarms, but would go back to normal. After about 10 minutes, it turned off,
leading Rob to plug out the plug from the back.
He ended up pulling the pin cable connector out two or three times and
plugging it back in before it turned on.
Then worked fine for about 10-15 minutes and suddenly turned off. Cleaned the pin connector with wire brush of
corrosion but that didn’t fix the problem.
Investigated the negative battery cable connection in the engine room to
ensure it had a good connection (which it appeared to be fine – just wiggled
the wire some and checked to make sure wingnut was tight on battery post) and
tried the power button and it came on.
Suspect the issue to be with the negative battery connection as that was
the previous problem in Marathon though visual inspection didn’t look like
anything was wrong.
6/10 - What is that smell coming from the bilge?! We've put fabric softener down there, we've cleaned what we can, but seriously cannot figure out for the life of us what that SMELL is! We are in an area that seems to have a high sulfur content as my sterling silver rings have tarnished while swimming and you can smell the sulfur when you put your nose into the sand. But, REALLY?!?! Do we have to have that smell oozing from our bilge?!
Hey you two!! WHen are we going to get new updates? What is happening out there? We all know you are hanging in DR with Moms in the meanwhile. Give us a new post when you can!
ReplyDeleteXOXOXO
Tasha & Todd